Foggy
Well-known member
We've been chasiing the soggy 60ft. times ever since we built this thing. Tried a lot of different stuff, converters, carbs (big/small), rear ends and traction control, with varying results; none great. So we pulled the motor out and down to freshen, and, add a new roller, with more leverage on the race side. We found evidence of bad valve train harmonics, intake mis-alignment, comb. chamb. issues, and even headgasget issues. But I believed we finally solved the poor 60ft. times, with a 10$ piece in the carb.:wtf: Still, the new cam, and prior issues were a need thing. We're also going to dyno this thing to get a real baseline.[smilie=::
And since we're hopefully knocking on the 9.99 sec. index, we thought it prudent to pull the 8pt. roll bars and install the 12pt. moly cage, and new steering box. Gone also, are the torsion bars in favour of the Strange coil-overs. And we still have the nitros system on board if we really want to make some real noise.
And since we're hopefully knocking on the 9.99 sec. index, we thought it prudent to pull the 8pt. roll bars and install the 12pt. moly cage, and new steering box. Gone also, are the torsion bars in favour of the Strange coil-overs. And we still have the nitros system on board if we really want to make some real noise.